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The inability to easily verify proper torque on the electrical connections to a power inverter charger and associated wiring in an RV can be dangerous. The vibrations from driving down the road and hitting bumps can loosen connections, resulting in heat and, potentially, fire. After seeing full-time RVing YouTubers HappilyEverHanks experience a fire and power outage due to a loose AC connection to their Victron inverter charger, Bob wanted to be proactive and ensure we had easy access to the wire connections to our Victron MultiPlus-II unit. This is vital as the unit provides uninterrupted power to our entire rig, whether we’re plugged in or camping off grid. Identifying the problem An inverter charger has two functions:
Because an RV is mobile, it’s imperative that an inverter charger is secured to the rig to minimize shaking as much as possible as the RV moves. When installing our Victron unit two years ago, Bob attached it to a shelf that ran the depth and width of half of the front compartment of our coach. He connected the unit to three lithium iron phosphate batteries underneath the shelf using bus bars to combine the positive wires and the negative wires. But there was no way Bob could get to the DC connections to check their torque without disassembling the setup. While I was out of town on a business trip, he got to work rewiring the Victron inverter charger to alleviate that problem. Changing the setup Fixing the issue required a complete change to our Victron setup. First, Bob disconnected all the wiring to the Victron unit and bus bars. Then he removed the Victron MuiltiPlus-II and the shelf that had held it in place. To be able to get to the connections, Bob cut the shelf down to 6 inches deep and shortened the width of it to allow space to connect the heavy-gauge wires to the three lithium iron phosphate batteries underneath. The batteries could stay on the bottom of the compartment as they were. But for optimal wiring, Bob had to reposition two of them. He reinstalled the adjusted shelf lower in the compartment, attaching it to the back of the cabinet. Then he beefed it up with angle iron running the length of it and added L brackets on each side for extra support. Bob mounted the 48-pound Victron unit on its side and attached it to the shortened shelf. Connecting the batteries After many painstaking hours, it was time to connect the batteries to the Victron unit. Together, the three batteries can carry up to 300 amps–100 each battery. Realizing that power required joining the batteries together–negative terminals to negative and positive terminals to positives. Bob connected the positives to one bus bar rated for 500 amps that he mounted on the ceiling of the compartment, and he connected the negatives to another 500-amp bus bar on the ceiling. The compartment may not look as pretty and clean as it used to, but Bob is breathing easier knowing he can periodically check the torque on the DC connections.
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4 Comments
Ray T Cole
2/19/2026 11:00:46 am
Good job!
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Gordie Johnsen
2/19/2026 01:42:48 pm
It takes a very knowledgeable Crew Chief like Bob to take on a challenge like this one. Good Job Bob!
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Betty Schoen
2/19/2026 04:02:05 pm
Holy Moly!! Bob, you are so brave and skilled. I would never even attempt that, as I'd wind up frying myself...not a way I want to achieve curly hair. I sure admire the skills you have. My Jeff is cerebral, and very intelligent about his line of work, but we do not hesitate to call the professionals for repairs and installs, as that is not a skill set for either of us. I wish my dad had recognized his fix it limitations... I didn't get that gene. Just 'splaining.
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Mom
2/22/2026 03:34:19 pm
Sounds like Bob knows what he’s doing. Better keep him around.
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AuthorThis is the travel blog of full-time RVers Bob and Lana Gates and our truck, Gulliver, and fifth wheel, Tagalong. Categories
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